RMS Olympic – Mutiny over
Titanic’s Boat Situation by Terry Randall
At the time of Titanic’s sinking,Olympic was on the return leg from New York of her fifth trans-Atlantic
voyage, having sailed from the United States at 1500 on Saturday 13th April 1912.
She did in fact pick up the distress calls sent our by her sister and started
to respond, but as she was on the southerly Atlantic route and over 500 miles
away from Titanic, the owners thought it best that the survivors did not
see the sister of the ship that had just sunk! So the diversion was called off.
Olympic arrived at Southampton in the early hours of Sunday 21st April to find
their home port in a state of mourning, but despite the all-pervading gloom,
activity in the dockyard was more intense than usual. At the White Star Dock,
she had to be prepared for her next scheduled departure, due three days later
on 24th April. In the light of recent events, considerable modifications were
to be made to the life saving apparatus on the boat-decks before departure.
Work immediately commenced to
embark 40 Berthon collapsible lifeboats, to ensure there was sufficient
lifeboat capacity for everyone on board. This was carried out under the
watchful eye of the Board of Trade Assistant Marine Surveyor at Southampton,
Captain Maurice Clarke; the man who had cleared Titanic for her sailing
less than two weeks earlier. The embarking of the extra boats came under the
direct supervision of White Star’s Marine Superintendent, Captain Benjamin
Steele. Orders for the actual number of boats needed seemed to change hourly
and at one point, after some 35 extra of these had been loaded, a message from
the Liverpool office of White Star arrived stating that in fact only 24 extra
boats were needed! As the surplus boats were landed ashore, rumours circulated
that the reason for their landing was because Captain Clarke had failed to pass
them as fit for use; two days later these rumours were to have a dramatic
effect!
By breakfast time on Wednesday
24th April,
the work had been completed, with the extra boats secured and covered. A number
of temporary wire falls had also been installed and extra deck hands had been
signed on to ensure that there were enough men to handle them. But despite the
Herculean efforts of the Harland and Wolff workforce at Southampton, in the end
their effort was for nothing.
Making an early start, Captain
Clarke went aboard at 0700 to inspect the new arrangements and give them an
even more thorough examination than he gave the davits on Titanic two
weeks earlier. As the passengers continued to arrive, he put the crew through
their paces, having them uncover and lower a number of different boats to make
sure that everything was in working order. The operation ran smoothly and
Clarke estimated that it took an average of only twelve and a half minutes to
lower each boat.
AT 1150, satisfied everything
was safe and on the verge of handing Captain Haddock his clearance to sail, a
message was rushed to the bridge informing the captain that his stokehold crew
was deserting the ship. A meeting was hastily arranged between the firemen and
a number of company managers, but unconvinced by Captain Clarke’s assurances
that the new boats were completely safe, the men refused to return on board
unless the company replaced the collapsible boats with conventional lifeboats.
There was no alternative but to
postpone the ship’s departure for New York until a replacement stokehold crew
could be mustered. Olympic was then moved to a safe anchorage off Spithead in
order to clear the berth, (also to make any further desertions impossible?)
while 2nd Engineer Charles McKean remained onshore to muster this new crew.
By dawn the next morning little
had changed; Olympic remained anchored in the Solent with steam up and
ready to sail. Not being one to waste time, Captain Clarke who had remained on
board in order to be able to give Olympic immediate „Clearance to Sail‟
the moment the new crew members arrived, he gathered a number of seaman on the
boat decks to practice boat drill yet again. This time the results were not so
reassuring, taking almost two hours to prepare and lower just a few boats. When
some of the passengers began to appear on deck at around 0800, the exercise was
stopped so that they would not be alarmed.
Later that morning the union
delegation arrived to negotiate a settlement to the dispute and after
discussions, six of the collapsible boats were lowered into the water and left
for two hours. On examination it was found that five were totally dry inside,
but the sixth did have a small amount of water in it. Closer examination
revealed a tiny hole*, but two hours of seepage could be easily bailed in less
than three minutes. After a quick conference in the captain’s cabin, the union
delegates agreed to advise their members that the boats were safe, provided the
faulty boat was replaced.
As
the afternoon wore on, with passengers on the decks in an increasingly
impatient mood, the management and engineers ashore continued to sign on
replacements, but it was not until 2200 that night that the tender finally
arrived alongside with a total of 168 replacement stoke hold crew. This number
included extra men considered adequate to allow Olympic to run at a
faster speed than normal, in order to make up some of the 36 hours already
lost.
It was but a temporary
reprieve! At midnight, as Olympic was preparing once more to put to sea;
another message arrived on the bridge telling Captain Haddock that more of his
crew were deserting. Now another 53 men (35 A/B’s, 5 Quartermasters, 5
Look-outs, 2 Lamp-trimmers, 4 Greasers and two other engine room personnel)
were boarding the tender that had brought out the new crew members; all refusing
to sail with the ship.
This time the problem was not
so much a lack of faith in the boats, but a lack of faith in the new crew! The
seamen regarded the new stoke hold crew as either ‘the dregs of Portsmouth’,or inexperienced firemen not experienced in the running of a large ship;
many of them did not did not even have “signing on‟ books!
Twice they refused Haddock’s
orders to return to their duties, though they acknowledged their sympathies to
him. A spokesman for the deserting seamen named Lewis admitted that the actions
of the firemen at Southampton had been “a dirty low down trick‟, but their replacements
were not fit to be aboard and that it would be unsafe to put to sea with them.
It was the last straw! Shortly
after midnight Haddock signalled the commander of the Royal Naval cruiser HMS
Cochrane lying half a mile away off Spithead:
“Crew deserting ship; request
your assistance. Haddock, Master.”
Within half an hour Captain W E
Goodenough RN had boarded Olympic to help mediate in the dispute and try
to persuade the men to return to their duties.
Although a number of the men
were still dissatisfied with the boats, the majority were more concerned at the
lack of experience in the new men; many of them were not even union members. It
was this last point that Captain Goodenough considered to be the root cause of
the new situation, believing that the men seemed to be more afraid of their
union than any possible repercussions from their actions. The threat of a
charge of mutiny failed to influence the men and the use of force could not be
considered as nobody had been hurt or threatened; in fact the men had shown
every respect for the two officers.
With a new stalemate on board,
the White Star management at Southampton wearily set about raising a new deck
crew in the early hours of the morning and at 1100 the tender again arrived
alongside with over thirty new men; though Captain Clarke failed to pass but a
few as fit for duty! A little over an hour later, Clarke received word from his
office to clear Olympic for departure as soon as he was satisfied the
ship was sufficiently manned, but with the ship already two days behind
schedule, this seemed less likely than ever.
At 1500, the expected news
to cancel the voyage arrived from the White Star Liverpool offices and Olympicreturned to Southampton to disembark her passengers. She would remain there
until her next scheduled voyage with union approved boats (and crew)
on the 15th May.
The mutiny was over, but for
the White Star Line, the entire incident following hard on the loss of Titanichad added insult to injury. If the company was ever to recover any of its
lost credibility, then action had to be taken; this action took the form of a
court case against the 53 seamen who had deserted the ship after sailing from
Southampton.
The case began on Tuesday 30th April in the
Portsmouth Police Court when the accused men answered to the charge that:
“…..they were guilty of wilfull
disobedience to the lawful commands of Captain Haddock, Master of the steamshipOlympic, contrary to section 225 of the Merchant Shipping Act, 1894.”
The defence lawyers based their
case on Article 458 of the same act claiming that as owners, the White Star
Line was obliged to ensure the seaworthiness of their ships, but in allowing Olympicto sail with an incompetent crew („the scallywags of Portsmouth’),
it almost amounted to rendering her as not seaworthy; as if she had a hole in her
hull!
Norman Raebarn, acting for the
White Star Line, called Captain Benjamin Steele the White Star Marine
Superintendent at Southampton, to testify that the life-saving equipment on
board was adequate and CaptainClarke
was subpoenaed by the company to testify that all the boats were seaworthy and
had an adequate number of seamen to handle them.
Regarding the competence of the
replacements, Second Engineer Charles McKean, who had mustered the new
stoke hold crew, admitted that many of the new men were inexperienced (many
were Yorkshire miners), but he did not consider the job of fireman to
be skilled labour, though he did admit much to the amusement of the court, that
it was hard work.
The verdict announced on 5th May went in
favour of the White Star Line, but in summing up the judge decided that it
would be inappropriate to fine or imprison the mutineers as they had probably
been „unnerved‟ by the recent Titanic disaster; it was probably as good
a result as the White Star Line was going to get. With attention now centred on
Lord Mersey’s enquiry in London into the loss of Titanic, the incident
was relegated to the background, as the company’s lawyers faced the more
daunting task of salvaging their employer’s reputation in a more public arena.
The one man who perhaps gained
from the mutiny was Captain Clarke. As Board of Trade Surveyor he was not paid
for any overtime, but his sixty hours marooned on Olympic had been above
and beyond the call of duty. He was given a bonus payment of £6-16-0 (£6-80p)
to compensate him for the extra work, which did a great deal to make up for the
three-day backlog that had built up on his desk while he had been away. The
extra cost was passed on to White Star in the form of an excess charge of £16.
The episode was over, but not
quite forgotten. On the 14th May a question was tabled in Parliament by George
Terrell MP ** to Prime Minister H H Asquith enquiring „what action if any,
was to be taken against the officials of the British Seafarers Union, who had
prevented the departure of Olympic, consequently delaying His Majesty’s Mails’.
Terrell’s question was referred to the Board of Trade, who unsurprisingly
decided, that as a result of the court case at Portsmouth, no prosecution was
worthwhile!
Olympic meanwhile remained at Southampton until midday 15th May, when she
sailed, without event, on the start of her sixth voyage to New York and back.
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*Rumour at the time (unsubstantiated)
was that it was possible to be able to push one’s finger through the sides of
these boats without effort.
**One cannot help but
speculate that this was probably prompted by White Star, in an effort to yet
exact some form of retribution against the so-called mutineers.
------------------------------------
George William Martell the 2nd was one of the
five Quartermasters involved at the time of the incident, also he was one of
the ship’s union representatives (the former British Seaman’s Union),
which probably explains his involvement in this episode. He returned to sea (discharge
book for that voyage, as with the other ‘mutineers’, being stamped ‘VNC’ Voyage
Not Completed!) mostly with Olympic, until as a Royal Naval
Reservist, he was remustered back into the Royal Navy at the outbreak of WW1.
He spent the whole of that war on minesweeping duties, an onerous and extremely
hazardous duty in what was in those days, still very much a new science in
naval warfare.
In 1916 his ship, HMS Beryl 2 (a
‘taken-up-from-trade’ vessel adapted for minesweeping duties), in which
he was “Ch/Bo “suns Mate – Coxswain”, was lost through enemy action, with his
captain being awarded the DSC and he himself the DSM. He was wounded during this
action and although he returned to active duty, finishing the war in the same
capacity in another minesweeper, his leg wound never completely healed; indeed
after the war and on his return to civilian life, it deteriorated even more so.
(Today’s modern drugs doubtless would have healed him!).
He died on the 28th February 1933
at the age of 53; his death considered by his widow to be directly attributable
to his wounds!
He was my maternal grandfather
and at the time of his death I was but six weeks short of my second birthday; I
wish I could have known him!
A
little story I remember my father relating, which really goes to show the
attitudes of people in those days, was that as George Martell got older, he
walked more and more with a pronounced limp and was thus a figure of fun, often
referred to behind his back as „bumble-foot George‟! To me he was a hero!!
T H Randall (Terry) 15th April 1931 - North Baddesley.